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Tuesday 26 January 2021

What is this?? The Amazon 2TB External SSD.

"You buy cheap, you buy twice"

An SSD was required for a Raspberry Pi project.  One was ordered from Amazon, 2TB. It was stupid cheap. 

It turns up...








It's plugged into the Pi, ready to clone the OS onto it... nope, not having it. Nothing detected... weird.

It's plugged in to a Windows PC... bing... a 2TB drive... there's a file on it, it's a word document. mustsee.doc. It's written in't fluent Yorkshire... 

What foolery is this??

Rat duly smelt. 

Let's investigate... 

Running Hard Disk Sentinel gives us some info... It's apparently a "Samsung HM201HI" ... except for a quick Google shows no such thing exists. Or is it 2 Samsung HM201HI's? It's also got some duff sectors on it. 

OK, let's run H2testw on it and see if it's really as big as it makes out... 


We may be here some time... 
As it turns out, we didn't have to wait as log as we thought... 
It had fallen over after 320 GB... 





So I sprung it apart ...
... and (no surprise) , it's a 320GB mechanical drive. 
It is, of course, a scam... 

Saturday 23 January 2021

Arduino Audio Compressor.

As part of an upcoming project, I need to compress some audio a bit. 

Now there's plenty of analogue compressor schematics on the web, but a lot require obsolete FETs or odd ball lamps, shining on an LDR (the optical compressor). I fancied a different approach.

Here's the plan, audio comes in to the "top" of a digital pot (also known as an R-DAC), the pot is controlled by the arduino. The wiper of the pot is connected to out audio output. That way, we can use the arduino to effectively wind our pot up and down to control the level of the audio. 

The wiper of the pot also feeds a rectifier, and the resultant level sampled by one of the Arduino's analogue ports, and that value is processed to provide the control signal to the pot.

A schematic is scratched out...


Audio comes in on J1, C3 is a DC blocking cap as the audio is biassed to half of the 5v supply by R1 & R2. The audio then feed the top of our digital pot, U2, on pin 5. Pin 7 of our pot is the bottom of our pot, and is connected to GND. Audio emerges from the wiper of out pot on pin 6, there's another coupling cap, C9, and the audio is then biassed to half our 12V rail by R14 & R16. It feeds a buffer amp, U1B and is output via R15 & C11, and is referenced to gnd by R17.The audio also feed U1A, which has a gain of about 14, and boosts the audio up to a sensible 10 volts pk-pk or so. This is coupled via C8 to our rectifier (D1 and a small filter cap of 10nF. This then drives the ADC of the arduino on pin A0. I haven't really shown the power supply, but it's just a single 12V supply, the 5V being derived from the arduino's on board regulator.

The software, can be found on my github page, as usual  https://github.com/andydoswell/audio-compressor

There are some variables to play with, being Target, Avg, Attack and Decay. Play around with the values and get a feel for it.

One other thing I played with, was feeding U1A from the incoming audio, rather than the devices own output. It was possible to get the software to lose control and end up with no audio coming out, but it could be tamed.. I think this type is called a "feed forward" compressor, and again, worth some experimentation. 


Here it is lashed on a bit of breadboard. It performed surprisingly well, and quiet too.


Thursday 21 January 2021

Linn Keltik repairs

As well as sending me a lingo (see here), John sent down a Klout amplifier... It had the same issues as this one, only was completely dead. A re-cap fixed it. 

It was also fitted with the Keltik Bass extension module. This is simply a low pass filter to allow the amplifier to drive a woofer as part of an active cross-over system. 

It's really nicely made, and was given a re-cap to ensure reliable service.


The Keltik module is mounted on a single metal spacer which bolts up to one of the four transistor heat spreader cap screws. Remove the spacer before attempting to remove the cap screw, or the whole thing locks up. The other end is supported in a groove on the speaker terminal output insulator.

There's a single connector to remove on the board.







We'll need to remove that screening can, which is simply desoldered. 










Same the other side...











.. to gain access to those hidden electrolytics.

Look at all those precision poly caps... nice!








You'll need 2 off 220uF 16V , 8 off 22uF 50V, 2 off 2.2uF 50V and 1 off 10uF 63V . 

They needed replacement, some were physically leaking, and smelt horrible during desoldering! 

Another saved from landfill! 

Saturday 16 January 2021

Linn Lingo repair - won't change speed.

John from the cold north rang...

"Got a Lingo here, it's been serviced by someone here, but it's now stuck in 33 RPM. Care to take a look?"

Yeah - why not?

It's the first version of the lingo.

Off with the lid, and I can see some work's already been done. It's been recapped. The workmanship is good... or is it?



The original repairer was obviously proud of his work, as there's a signed sticker inside the unit. I've blurred this out to prevent embarrassment. 





Now the lingo is similar to other power supplies of this era from linn, they suffer with capacitor failure. Now you could upgrade your supply to the latest and greatest (don't forget kids, Linn ownership is all about upgrades, right?), or get it repaired. This has all new capacitors, of quality brand, so it should be good. It was only done in August last year (it's now January). Apparently 45 RPM hasn't worked since they had it back... 


So it's just stuck in 33. Pushing and holding the switch just causes the Red led to go from bright to dim repeatedly, and never get to 45. Great ... it's usually either U7 or U8, best to change both to avoid issues. It's a 74LS74. The best way to get them out is to cut off the legs, and remove each leg separately to avoid damaging the (as usual) fragile double-sided print. I get two new IC's and socket them. Powering back up, and switch to 45 , it briefly lights the green 45 RPM light, before dropping back to the original fault. Damn. 

Thankfully having socketed the IC's, I can remove them without damaging them, and test them in the sometimes useful DiagnoSYS IC tester (thanks Norm).

One is duff... double damn... was it a duff one out of the packet? I replace it, and promptly blow another. Triple damn. What's going on?

There's a bit of feedback from the motor drive amplifier on the lingo, so it knows when to turn the voltage down to the motor. This feeds U4, a 74LS221. It's removed , and a socket fitted. A new chip changes the fault slightly. Sadly the DiagnoSYS tester can't do 74LS221's..  Checking U7 again shows it hasn't failed again, so that's something. Out with the scope. There should be a ~5 second timing constant. Checking around, I find it. It's on pin 6 of U4... and is formed by C7 (220uF) and and R33 (56K) (those of you who have just got the calculator out, will inform me that that's 12 seconds, and yes, you're right, but it triggers the IC as it moves over the trigger threshold, of around half of the supply). The cap is obviously brand new, but is removed anyway and tested. It tests fine. But it's only 22uF. C7 and C9 have been reversed!! (now you know why I blurred the label!).

It's reassembled again, and this time works fine! 


















"The person that never made a mistake, never made anything" 

Ahem.. 



Saturday 2 January 2021

Heathkit Stereo control unit USC-1

Happy New Year! 

Having sorted the MA-12's, time to move onto to the USC-1 preamp...


It's designed to be mounted into the front of a cabinet of some description. 


They keen-eyed amongst you may notice the absence of mains transformer. The power supply is derived from the MA12 amplifier via a multi-pin lead. 


It's a reasonable layout, but the chassis edges are sharp. There's two PCBs, each containing Two EF86's and an ECC83. The EF86's produce two diferent levels of gain, one setting for TAPE1/2, GRAM and MIC, and the second stage conntecting the inputs from RADIO and AUX. There's no real RIAA equalisation on the GRAM but a little bit of loading. The second EF86 feeds a tone stack, which is then amplified by one half of the ECC83, followed by the other. There's also a low pass filter implemented here. It's full of horrible Hunts... 

The base is removed to gain access to the solder side.











... and a good while spent changing all those nasty caps out...











I chose not to re-stuff the can on this occasion, as there's a nice bit of tag strip that forms the power supply filter, so they could just be mounted there ...









At some stage in the past, the volume control has been replaced, for one without a switch. It's also been wired up backwards. It's now wired up correctly, so as not to deafen the unsuspecting user.

How's it sound? I thought there would be more "blow" due to the EF86's cascaded, but it's reasonably quiet. Obviously the TAPE setting is nothing more than a head amplifier, so not suitable for a line level output from a modern deck.  Pity about the RIAA, or lack thereof...*  Tone controls are actually very nice, and don't offer too much cut or boost. 

The switch-gear is lovely, and has stood the test of time really well. 

*upon reading the manual, it transpires the input stage was designed for a Decca FFSS cartridge, the manual does give some suggestions about use with other carts. 

Wednesday 30 December 2020

Heathkit MA-12 Hifi amplifier restoration.

Neil called ...

"Got a load of old 'eathkit gear here , could use the once-over... Care to have a look?"

Yeah... why not?

There's four MA-12 amplifiers, two USC-1 "Stereo control units" (that's a pre-amp to you and I), and an AMF1 tuner ...

The amps are in various states of repair ...



Including one with a valve down to air ...












It's a simple push-pull amp, with an EF86 front end, an ECC83 (12AX7) phase splitter and a pair of EL84's wired ultra-linear. Hmmm , we've seen that before, and looking at the schematic, it's a Mullard 5-10 in disguise..




Off with the bottom ... 












Nice tag-strip construction, and, as these were sold as kits, the assembly looks OK.. some of these can be a disaster area.


Obvious faults... it's full of Hunts capacitors (evict on sight) , and the electrolytics are, well.. past it.











First things first, get that can out, and re-stuff it with nice modern parts ....

The cap is simply removed by gently prying it out with a screwdriver, and saving it.







Next drop the whole can into a container of boiling water for about 15 mins...











Wind a screw into the capacitor's innards ... 


and extract! Probably best wearing some gloves whilst you're doing this bit, I don't know what chemicals are in there ... 









This can is a dual 250uF, 60uF , 350V device. I've got a modern 220uF and a 68uF to go in there, so this is assembled and wired... 










.... and slid back into the can. The cap is sealed on with a little RTV.

The other can is a dual 50+50uF. As it's rubber cap is visible, we want to leave that intact. 

So the bottom bracket is warmed up slightly, and pried off.. 
and the bottom but off with a small pipe cutter... 

It's stuffed with two 47uF caps. They're slightly different shapes so they fit inside the can. 
The base is then sealed up with a splodge of hot-melt. 

The Hunt's are evicted and replaced with some nice polys. 











The two cathode bypass electrolytics (22uF, 25V) are replaced.











Testing shows the output is weak (our valves may be old), and unacceptable distortion...










Attention is turned to the output stage ... 

DC conditions on the two valves should be closely matched... they're not.








The two cathode resistors R21 and R22 have risen significantly in value, one to more that 3 times it's value, they're swapped out. R23 and R24, the screen gird resistors, are also out of spec. Changing this lot puts matters right. 

Now to do the other three! ....